|   | 
        | 
        | 
    
     
      |   | 
       | 
        | 
    
     
      |   | 
      K  r  i  e  
          g  s  t  a  g  e  b  u  c  
          h  | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      " U-107  "  | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      Machine Section  | 
        | 
    
     
      |   | 
      War patrol from 21.4. to 11.7.1942 
          (6th War Patrol)  | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      A.)  1.)  Diesel power plant failures - cooling 
        water pumps, starboard exhaust gas valve, fuel oil loss, lubricating oil 
        purifier failure. | 
        | 
    
     
      |   | 
              2.)  Aft 
        diving plane failed. | 
        | 
    
     
      |   | 
              3.)  Distilling 
        unit's vapor pump failed. | 
        | 
    
     
      |   | 
              4.)  Trim 
        pump out of service. | 
        | 
    
     
      |   | 
              5.)  Main 
        drain pump buzzing sounds, leaking. | 
        | 
    
     
      |   | 
              6.)  Both 
        negative buoyancy tanks leaking. | 
        | 
    
     
      |   | 
              7.)  Conning 
        tower hatch leaking. | 
        | 
    
     
      |   | 
              8.)  Quick 
        vent valve of main ballast tank 7 starboard leaks. | 
        | 
    
     
      |   | 
              9.)  Battery:  
        Abnormally heavy water consumption, efficiency heavy degraded. | 
        | 
    
     
      |   | 
            10.)  Junkers compressor 
        failed. | 
        | 
    
     
      |   | 
            11.)  Port head valve 
        multiple leaks. | 
        | 
    
     
      |   | 
            12.)  Minor failures. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 1:  a)  When inspecting the diesel 
        engine cooling pumps on 9, 11 and 13 June, looseness of the retaining 
        brackets of the port pump's inlet valve, and the starboard pump's inlet 
        and output valves was eliminated. On 16 June, knocking noises appeared 
        in the starboard pump.  After immediately stopping the engine an 
        investigation was conducted, which showed the following: | 
       | 
    
     
      |   | 
              The retaining 
        bracket was broken and the starboard external inlet valve's seat was badly 
        damaged.  | 
        | 
    
     
      |   | 
      Probable cause: | 
        | 
    
     
      |   | 
              Breaking of 
        the valve seat rings. Pump had to be stopped. The repair took 3.5 hours. 
        Otherwise, the new drives (hardened shafts) of both cooling water pumps 
        have been working without any problems. | 
        | 
    
     
      |   | 
                    
        b) Spindle guide, grinding gear and stuffing box of the internal, starboard 
        exhaust valve leaks quite heavily despite tightening.  When the starboard 
        valve is closed during submerged cruise, after cooling down, the water 
        leak in the exhaust manifold is even greater.  The turbo-blower casing 
        and valves must be replaced.  Despite frequent lubrication, the starboard 
        valve is very hard to operate.  Crash diving takes twice as long. 
          There is water in the cylinders of the starboard engine.  
        The increasing level of water in the starboard collecting tank over approximately 
        1% is compensated for by cruising at higher RPM.  On the basis of 
        the indicator diagram and the exhaust's color, it seems that the piston 
        rings must be replaced due to water leaks. | 
        | 
    
     
      |   | 
                    
        c) From 10 to 12 June the following fuel oil loss was determined: | 
        | 
    
     
      |   | 
                    
        Port 1 internal 5 m³ (cause not clear, not used previously, refueling 
        performed normally) | 
        | 
    
     
      |   | 
                    
        Starboard 1 internal, 1.5 m³ (probably leaks during fuel transfer 
        to collecting and gravity tanks) | 
        | 
    
     
      |   | 
                    
        Starboard 2 internal 1 m³ (unexplained) | 
        | 
    
     
      |   | 
      Refueling according to the Flotilla Chief Orders.  
        Oil flew from the test lines.  Cooling water pump used.  No 
        oil leaks. | 
        | 
    
     
      |   | 
                    
        d)  During last overhaul of the boat in the yard the lubricating 
        oil purifier was exchanged with one taken from another boat.  There 
        is a leak in the loose valve seat ring over the neck journal bearing, 
        and as a result, the bearing, worm gear and the shaft were running in 
        a mixture of the lubricating oil and water. After 24 hours of continuous 
        operation, the purifier stopped with a buzzing noise.  The teeth 
        of the worm gear were broken out for half of their length.  Repair 
        was not possible by on board means. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
        | 
        | 
        | 
    
  
  
     
      |   | 
        | 
        | 
    
     
      |   | 
      - 2 -  | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
                    
        e)  Due to spring fatigue (opened at 0.9 kg/cm² and did not 
        close) - despite immediately stopping the diesel engine - the starboard 
        cooling water safety valve caused a large water intake in diesel engine 
        room.  The spring tension was increased by inserting a 3 mm thick 
        gasket. The repair took 1 hour.  The valve is tight. | 
        | 
    
    
      |   | 
        | 
        | 
    
     
      |   | 
      To A 2:  On 3 May the aft diving planes jammed in 
        the “hard up” position due to limit switch failure. The boat 
        was trimmed on an even keel and the limit switch was removed. The switching 
        axle of the switch was rusted and eroded in the stuffing box.  The 
        diving planes spindle was moved to the neutral position by means of tackle 
        and crowbar and a new limit switch was installed. The repair took 8 hours. | 
        | 
    
     
      |   | 
              On 31 May during 
        a submerged attack, the aft diving planes driving motor windings started 
        to smoke. The driving motor was flooded with lubricating oil from the 
        gear box, through the radial shaft seal of the full-floating axle. The 
        commutator sparked strongly.  | 
        | 
    
     
      |   | 
              The motor was 
        disassembled, thoroughly cleaned, the resistance of the armature and field 
        windings measured, commutator removed and cleaned, and the brushes replaced. 
          After lowering the lubricating oil level in the gear box down to 
        the half of the height of the inspection hole, no further failures occurred. 
          The repair took 30 hours.  The boat had to be submerged to 
        mount the motor, for this purpose, removing of the manual driving shaft 
        gear was necessary. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 3:  On 12 June a buzzing noise occurred 
        in the vacuum pump.  | 
        | 
    
     
      |   | 
      Due to slight bearing looseness, the working and control 
        pistons of the pump blocked each other, which led to breaking of the gear 
        teeth of the drive gear and drive shaft at the point of passing through 
        the casing.  After removing both pistons, the pump casing openings 
        were closed with flanges and the evaporator started working as over-pressure 
        distilling unit.  | 
        | 
    
     
      |   | 
                                         
        Overpressure:         0.1 kg/cm² | 
        | 
    
     
      |   | 
                                         
        Capacity:               
        100 liters/day | 
        | 
    
     
      |   | 
                                         
        Salinity:                
          6 - 8 mg/liter | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 4:  After a short time of operation, knocking 
        noises occurred in the trim pump, similar to those during the previous 
        war patrol, which led to the misaligning of the drive motor and pump shafts 
        (Goal of the repair: aligning the shafts).  Up to 13 June rubber 
        sleeves of the coupling, destroyed by working, had to be replaced 4 times. 
          On 13 June the bearings of the worm shaft were warmed up to high 
        temperature and knocking occurred.  After lifting and suspending 
        the driving motor, the worm shaft with bearings and worm gear could be 
        dismounted.  Sea water had leaked into the crankcase through a cracked 
        cooling coil.  The worm gear as well as the ball bearings were heavily 
        rusted and corroded.   The bronze worm gear was heavily worn on its 
        edges.  Bronze mud was in the crankcase. | 
        | 
    
     
      |   | 
      The cooling coil was closed with flanges and the ball bearings 
        set up for lubrication with grease. After assembly, the pump was run for 
        a short time without any serious increase in the temperature of the bearings 
        or any loud noise.  It must be considered why the oil can not be 
        exchanged without pump disassembly, if grease lubrication is safe for 
        the ball bearings and the drain screw of the crankcase is so inconveniently 
        located.  The repair took 70 hours. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 5:  On 23 April when starting the main 
        drain pump, especially when submerged and when pumping from pressurized 
        regulating tank, a knocking noise occurred in the separating chamber caused 
        by the ball of the check valve.  The check valve and venting cock 
        must not have been air tight. Multiple grindings of the leaking vent cock 
        and check valve did not remove the problem.  When attaining greater 
        depth, the vent lines has to be wedged with wooden plugs to prevent large 
        water leaks (pump remains under external water pressure, because the main 
        drain pump suction hull valve and intake of the main drain pump are leaking). | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
        | 
        | 
        | 
    
  
  
     
      |   | 
        | 
        | 
    
     
      |   | 
      - 3 -  | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 6:  Since 15 May, both negative buoyancy 
        tanks leak.  They flood when external sea water pressure increases; 
        when pressure decreases, they leak or vent outboard.  By pressurizing 
        the tanks or venting them inside the boat, corresponding to the depth, 
        the tanks are made makeshift tight. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 7:  The leaking conning tower hatch admits 
        water until periscope depth is achieved, can not be sealed by setting 
        the hatch dogs in their stop position.  The hatch gapes over ¼ 
        of the perimeter length.  The hatch and the frame must be adjusted 
        precisely in the yard or the frame must be milled. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 8:  On 12 May, while blowing, heavy leaking 
        of quick vent valve chamber 6/7 in the upper deck was discovered.  
        Part of the rubber seal of the valve disc of the starboard tank 7 was 
        cracked at the external hinge and jammed between the seats.  The 
        valve disc was disassembled and the rubber seal was replaced.  The 
        repair took 2.5 hours. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 9:  The last battery capacity test performed 
        in Lorient showed an efficiency of 75%.  During this patrol, especially 
        after failure of the distilling unit, due to abnormally heavy distilled 
        water consumption by individual cells, serious troubles occurred. | 
        | 
    
     
      |   | 
       Probably some cells have internal short-circuits, caused 
        by lead mud, which – as well as sulfation – have significant 
        impact on the output voltage.  These cells have to be renewed or 
        desludged. | 
        | 
    
     
      |   | 
       On 8 July, the battery was charged for 3.45 hours at 600 
        Ah, until generating oxygen and hydrogen. According to the machine log, 
        there should be at least 10274 Ah available.  After withdrawal of 
        4944 Ah for driving motors, 2070 Ah for the boat's equipment and 165 Ah 
        for losses, after 12 hours submerged cruise, there should be 3155 Ah remaining 
        available. | 
        | 
    
     
      |   | 
       At 23.10 hours, the main switch board voltmeter showed 
        109 V, which corresponded to about 1500 Ah while cruising at slow speed. 
          After reaching periscope depth at half speed with both motors at 
        23.13 hours, voltage decreased to 94 V immediately.  The diving planes 
        driving motors stopped working at such a low voltage supply, and the diving 
        planes remained in the following position: forward – hard up, aft 
        – down 10°.  The broadcast and announcement system also 
        failed.  The boat was not under control and had to be surfaced immediately. | 
        | 
    
     
      |   | 
      Available Capacity:  7119 : 10274= 69% | 
        | 
    
     
      |   | 
      Ratio to target capacity:   7119 : 12150 
        = 58% (50 hour-current) | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 10:  Total operating time: | 
        | 
    
     
      |   | 
                
              Since last overhaul: | 
        | 
    
     
      |   | 
                    
        a) After disassembly of the internal exhaust gas valve, it was found that 
        the seat of the valve was burnt or ground out over half of its perimeter.  
        Repair was not possible by on board means.  The external valve is 
        tight.  | 
        | 
    
     
      |   | 
                    
          b) On 13 May, the air compressor did not start.  The fuel pump 
          plunger had been jammed during fuel priming.  Due to wear of the 
          regulating spindle, it had canted when moving.  As a result a lateral 
          force acted on the teeth of the pump plunger, which led to jamming of 
          the plunger.  The regulating spindle was fixed by means of the 
          guide screw and jamming was thereby prevented.  The shut-off gear 
          on the safety valve was thus blocked.  The repair took 12 hours. 
         | 
        | 
    
     
      |   | 
                    
        c) On 25 April, the compressor had to be stopped, because of damage that 
        occurred in stages 3 and 4.  After disassembly of the intake nozzles 
        of the stage 4, iron shavings were found between the valve disc and valve 
        seat, which caused pressure discharge from the stage 4 to stage 3. The 
        origin of the iron shavings was not possible to determine.  Stages 
        3 and 4 were completely operable.  After a 20 minute test run, the 
        same damage as described above occurred.  After multiple starts of 
        the compressor, the stages 2, 3 and 4 did not receive starting air.  
        The compressor could not be started.  As a cause, it was determined 
        that the ball of the check valve of the starting air line leading to stage 
        2 was jammed and prevented flow of the starting air.  The examination 
        of the check valve showed, that the valve seat and fitting spring were 
        damaged.  The failure in stages 3 and 4 is explained as follows: 
        after failure of the fitting spring and the seat of the check valve of 
        the starting air line for stages 2, 3 and 4, the valve's ball was swirled 
        by the flowing compressed air (line illegible) | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
        | 
        | 
        | 
    
  
  
     
      |   | 
        | 
        | 
    
     
      |   | 
      - 4 -  | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      compressed air through the compressor and caused the valve 
        damage.  The repair took 15 hours.  | 
        | 
    
     
      |   | 
      The newly installed cooling water pump and automatic starting 
        gear were running without any problems. | 
        | 
    
    
      |   | 
        | 
        | 
    
     
      |   | 
      To A 11:  On 3 and 28 June, during crash dives, 
        for an unknown reason, the port head valve was jammed about half way to 
        “closed” position.  The valve must be disassembled in 
        the shipyard. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 12:  a)  Due to contamination in 
        the high pressure compressed air installation caused by iron shavings 
        (see damage 10 c), the valve seats of the main blowing valve and regulating 
        and negative buoyancy tanks blowing valves had to be overhauled multiple 
        times. | 
        | 
    
     
      |   | 
                    
        b)  On 22 April in stage 3 of the electric compressor pressure increased 
        abnormally.  In stage 2 pressure increased at a smaller rate, jammed 
        inlet and delivery valves in stage 3 were replaced.  The repair took 
        1.5 hours. | 
        | 
    
     
      |   | 
                    
        c)  The loose clamping screws and scorched contacts of the relay 
        in the diesel engine room engine order telegraph receiver caused momentary 
        rattle in the starboard engine order telegraph in the electric motor room. 
          The repair took 4 hours. | 
        | 
    
     
      |   | 
                    
        d)  The hull valves of the blowing lines leading to tanks 7 starboard, 
        6 port and 4 starboard were improperly sealed with non-oil-tight material 
        (hemp) and were leaking.  They were sealed with asbestos-graphite 
        and since then they are tight. | 
        | 
    
     
      |   | 
                    
        e)  Despite especially frequent and thorough draining, 6 cartridge 
        type, pressure reducing valves of type D 2500 (Dräger) were damaged 
        by water hammer effect.  Evidently their construction is too sensitive 
        for pressurized water. | 
        | 
    
     
      |   | 
                    
        f)  Despite appropriate rollers, the port shaft revolution transmitter 
        failed because the drive chain slipped off even at normal bow down angles.  
        Damage is typical. | 
        | 
    
     
      |   | 
                    
        g)  Aerial bomb damage | 
        | 
    
     
      |   | 
                
                 On 15 May, one aerial 
        bomb, starboard abeam.  Damaged fuses and fuse sockets, as well as 
        lamps.  Log indicator and depth meter in the conning tower are out 
        of operation. | 
        | 
    
     
      |   | 
      B.)         a)  
        Nothing of note.   | 
        | 
    
     
      |   | 
                    
        b)  1:  Consumption of lubricating oil at a level of 
        3% shows, that newly installed piston and oil rings are correctly aligned. 
        The heavy smoke of the starboard engine at end of the patrol was caused 
        by flooding the cylinders with sea water two times.  Some of the 
        failures described in paragraph A I should not have occurred after overhaul 
        in the shipyard, which went on for 5 weeks. | 
        | 
    
     
      |   | 
                         
        2:  Breakdown A 4  shows, that a second auxiliary 
        drain and trim pump (piston type pump) would considerably increase the 
        safety of the boat.  All previous patrols show, that in case of damage 
        of the trim pump, draining of the bilges in the end compartments by the 
        centrifugal pump is unreliable. | 
        | 
    
     
      |   | 
                         
        3:   Breakdown 12 e  shows, that especially when 
        the boat operates in the tropics, it seems advisable that sensitive low 
        pressure regulators should not be connected to the lowest outlets of the 
        high pressure air distributor to avoid carrying away accumulated water. | 
        | 
    
     
      |   | 
                         
        4: Refueling of 43 m³ fuel oil from “U-459” was 
        conducted quickly and without problems. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
        | 
        | 
        | 
    
  
  
     
      |   | 
        | 
        | 
    
     
      |   | 
      - 5 -  | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
                         
        5:  With plugged drain connections in the diesel engine room, 
        there is no possibility of draining the bilges with the trim pump by means 
        of a flexible hose.  A moderate amount of necessary threaded fittings 
        would increase the safety in case of a water leak. | 
        | 
    
     
      |   | 
                         
        6:  The plexiglas water level gauge of the regulating tanks 
        and the plexiglas tube for the Papenberg instrument, which were installed 
        during last overhaul in the yard, did not break when the aerial bomb exploded 
        quite near.  | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      
           
            |   | 
            Port Motor  | 
             | 
            Starboard Motor  | 
           
           
            |   | 
              | 
              | 
              | 
              | 
              | 
              | 
              | 
           
           
            |   | 
            Days  | 
            Hours  | 
            Min.  | 
             | 
            Days  | 
            Hours  | 
            Min.  | 
           
           
            |   | 
             | 
             | 
             | 
             | 
             | 
             | 
             | 
           
           
            | Total operating time since commissioning: | 
            220  | 
            18  | 
            33  | 
             | 
            221  | 
            15  | 
            30  | 
           
           
            |   | 
             | 
             | 
             | 
             | 
             | 
             | 
             | 
           
           
            | Total operating time during the last patrol: | 
            37  | 
            7  | 
            37  | 
             | 
            37  | 
            22  | 
            15  | 
           
           
            |   | 
             | 
             | 
             | 
             | 
             | 
             | 
             | 
           
           
            | Revolutions since commissioning: | 
            83  | 
            148  | 
            596  | 
             | 
            84  | 
            922  | 
            374  | 
           
           
            |   | 
             | 
             | 
             | 
             | 
             | 
             | 
             | 
           
           
            | Revolutions during the last patrol: | 
            13  | 
            398  | 
            180  | 
             | 
            14  | 
            144  | 
            920  | 
           
           
              | 
              | 
              | 
              | 
              | 
              | 
              | 
              | 
           
          | 
        | 
    
     
      |   | 
      Reached diving depth:  A +60 meters. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      B.)  Consumption: | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      Fuel measured run, see enclosure. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      Commissioning of the boat 8.10.1940 | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      Presented:                                                                   
        The Chief Engineer | 
        | 
    
     
      |   | 
      signed in draft  G e l h a u s                                         
        signed in draft  B ö e r | 
        | 
    
    
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      Kaptlt. and Kommandant                                            
        Kaptlt. (Ing.) | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
       | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
        | 
        | 
        | 
    
  
  
     
      |   | 
        | 
        | 
    
     
      |   | 
       | 
        | 
    
     
      |   | 
      Flotilla Remarks: | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 1 a)  This damage was probably caused 
        by broken seat rings, which in turn was caused by loose retaining brackets 
        of the seats of the inlet valve. | 
        | 
    
     
      |   | 
      1 b)  Cause of the water intake: rupture in the cooling 
        flange of the turbo-blower, between the turbine and blower (2nd case in 
        last half of year).  The repair was done by welding, the flange must 
        be renewed. | 
        | 
    
     
      |   | 
      1 c)  The loss remains unexplained; while refueling 
        the internal fuel oil tank, its capacity was measured and it was stated, 
        that it was completely filled. | 
        | 
    
     
      |   | 
      1 d)  The shield of the neck journal bearing was not 
        sealed properly. | 
        | 
    
     
      |   | 
      1 e)  The cooling water safety valve which quite frequently 
        causes a water leak in the diesel room bilge must be tested at regular 
        intervals (about weekly).  Only in that way, can one prevent surprises. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 2 a)  An inspection of the switch remains 
        indicates that sea water entered the limit switch, either through an improperly 
        installed cover, or through a defective stuffing box. | 
        | 
    
     
      |   | 
      2 b)  Defective radial shaft seal; isolated case. | 
        | 
    
    
      |   | 
        | 
        | 
    
     
      |   | 
      To A 3)  In the case of mechanical damage to 
        the vapor pump, attempts at repair are hopeless; in such a case, there 
        is the possibility of running the distilling unit as an over-pressure 
        unit, which should be considered on all boats. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 4)  The driving motor was not aligned 
        with the pump, which led to the destruction of the flexible coupling. 
          The pump ran roughly and noisily.  Alignment is difficult 
        to perform because there are no fitting bolts provided for the motor. 
        The breaking of the condenser coil was probably connected with the vibration 
        caused by rough running. When overhauling the pump in the yard, the ball 
        ring of the ball bearing was discovered damaged; it remains unexplained, 
        if it was damaged during assembly of the pump on board or earlier and 
        sped up the destruction of the worm gear. - New worm gear. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 5)  After repair of the check valve and 
        venting cock the pump operates without problems. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 6)  The corroding of the vent line of 
        the tanks, just under the vent valves reappeared again!  It appears 
        more frequently than expected, there is a need to install line with thicker 
        walls. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 7)  To the longstanding request to make 
        conning tower hatch bearing stronger and more stable, it is noted, that 
        after installing double spring, hatch failures will be rare. - This boat 
        will be first one on which the double spring will be installed. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 8)  Isolated case. | 
       | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 9)  The battery of the boat must be considered 
        exhausted.  By forming up, especially in the forward battery, all 
        cells, even those which by means of previous output voltage measurement 
        were indicated as damaged, were charged to the same voltage.  Capacity, 
        however, was low and its value (at 20 hour current) was: forward battery 
        64%, aft battery 61%.  By performing multiple charging and discharging 
        cycles, it was determined, that an output voltage of 146 V could not be 
        exceeded.  Up to that voltage, the temperatures were within moderate 
        limits (30-35C), with additional charging at a voltage of 146 volts, the 
        temperature rose in a short time until reaching a final value of 45C.  
        During the current war patrol – to avoid achieving this high temperature 
        and resulting high water consumption - generally, charging up to generating 
        oxygen and hydrogen was not performed.  The battery then had to be 
        deeply discharged, to reform it again.  After this patrol, replacement 
        of the battery (in connection with thorough overhaul) is scheduled. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
      To A 10 c)  An investigation to determine the cause is being 
        conducted. | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
      |   | 
        | 
        | 
    
     
        | 
        | 
        |