To A X ; 1. |
On 10 February the pressure fell in the pressure water installation. Examination showed that the test piping from the high reservoir was broken before the pressure hull pass trough. The break point was heavily rusted. The test valve in the diesel room was closed. The damage was corrected. The test piping remained out of service. |
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To A X ; 2 |
The gasket rings in the fuel vent had to be renewed very often. The rubber was completely disintegrated, despite asbestos wrapping. The rings were replaced with new. You would have to try copper asbestos rings |
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To A I ; 3 |
A fuel valve cooling tube on the starboard engine broke at the bolt connection. Replaced with a spare. |
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To A II ; 1 |
In 27 February the cooling installation of the aft air cooler in the E-motor leaked, although it was overhauled and pressure tested during the shipyard period. The cooler was opened up. One cooling coil was blind flanged, because overhaul was not possible. Duration 5 hours. |
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To A III ; 1 |
On 28 February after running the compressor for one hour strong knocking was determined. The babbitt of the crank bearing half at the foot of the connecting rod of compressor stage II was worn. The red brass unbore half crank bearings were normal. Examination showed that the oil supply from the support bearing was interrupted. An unidentified foreign body had closed the oil conduit with feed hole. The support bearing was replaced with a spare. The crank bearing half at the foot of the connecting rod was lined with bearing metal and refitted. The compressor ran up to the end of the operation without malfunction. |
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To A III ; 2 |
On 1 March it was determined that the vent of the forward ballast tank was blocked open. The indicator on the oil pressure meter was in the "closed" position. Manual operation found the restriction in the limit switch. After opening the manhole on the upper deck, it was found that a wedge was missing and that a second wedge in the operating linkage was completely worn out. The joint pieces were removed and installed with newly made wedges. Duration 12 hours. |
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To A III ; 3 |
On 4 March a 2 mm hole was found in the blowing line of the rear ballast tank in the upper deck. The defective part had rested through and was positioned in such a way that the cell is slowly venting. It was quickly covered with a rubber pad and bolted over the hole. Further venting was not observed. |
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